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Dennis Donovan

(18,770 posts)
Tue Sep 3, 2019, 08:45 AM Sep 2019

94 Years Ago Today; Navy zeppelin USS Shenandoah destroyed in squall over Ohio

https://en.wikipedia.org/wiki/USS_Shenandoah_(ZR-1)


USS Shenandoah moored at NAS San Diego

USS Shenandoah was the first of four United States Navy rigid airships. It was constructed during 1922–23 at Lakehurst Naval Air Station, and first flew in September 1923. It developed the U.S. Navy's experience with rigid airships, and made the first crossing of North America by airship. On the 57th flight, Shenandoah was destroyed in a squall line over Ohio in September 1925.

<snip>

Crash of the Shenandoah

On 2 September 1925, Shenandoah departed Lakehurst on a promotional flight to the Midwest that would include flyovers of 40 cities and visits to state fairs. Testing of a new mooring mast at Dearborn, Michigan, was included in the schedule. While passing through an area of thunderstorms and turbulence over Ohio early in the morning of 3 September, during its 57th flight, the airship was caught in a violent updraft that carried it beyond the pressure limits of its gas bags. It was torn apart in the turbulence and crashed in several pieces near Caldwell, Ohio. Fourteen crew members, including Commander Zachary Lansdowne, were killed. This included every member of the crew of the control car (except for Lieutenant Anderson, who escaped before it detached and fell from the ship); two men who fell through holes in the hull; and several mechanics who fell with the engines. There were twenty-nine survivors, who succeeded in riding three sections of the airship to earth. The largest group was eighteen men who made it out of the stern after it rolled into a valley. Four others survived a crash landing of the central section. The remaining seven were in the bow section which Commander (later Vice Admiral) Charles E. Rosendahl managed to navigate as a free balloon. In this group was Anderson who—until he was roped in by the others—straddled the catwalk over a hole.

The Shenandoah Crash Sites are located in the hillsides of Noble County. Site No. 1, in Buffalo Township, surrounded the Gamary farmhouse, which lay beneath the initial break-up. An early fieldstone and a second, recent granite marker identify where Commander Lansdowne's body was found. Site No. 2 (where the stern came to rest) is a half-mile southwest of Site No. 1 across Interstate 77 in Noble Township. The rough outline of the stern is marked with a series of concrete blocks, and a sign marking the site is visible from the freeway. Site No. 3 is approximately six miles southwest in Sharon Township at the northern edge of State Route 78 on the part of the old Nichols farm where the nose of the Shenandoah's bow was secured to trees. Although the trees have been cut down, a semi-circular gravel drive surrounds their stumps and a small granite marker commemorates the crash. The Nichols house was later destroyed by fire.


The wreck of the Shenandoah Crash Site No. 3


The wreck of the Shenandoah Crash Site No. 2

Two schools of thought developed about the cause of the crash. One theory is that the gas cells over-expanded as the ship rose, due to Lansdowne's decision to remove the 10 automatic release valves, and that the expanding cells damaged the framework of the airship and led to its structural failure.

Aftermath
Looting

The crash site attracted thousands of visitors in its first few days. Within five hours of the crash more than a thousand people had arrived to strip the hulk of anything they could carry. On Saturday, 5 September 1925, the St. Petersburg Times of Florida reported that the site of the crash had quickly been looted by locals, describing the frame as being "[laid] carrion to the whims of souvenir seekers". Among the items believed to have been taken were the vessel's logbook and its barograph, both of which were considered critical to understanding how the crash had happened. Also looted were many of the ship's 20 deflated silken gas cells, each worth several thousand dollars, most of them unbroken but ripped from the framework before the arrival of armed military personnel. Looting was so extensive that it was initially believed even the bodies of the dead had been stripped of their personal effects, and that operatives from the Department of Justice were being sent to investigate. That this was happening was soon denied by those publicly involved in the incident, however. Still, a local farmer on whose property part of the vessel's wreckage lay began charging the throngs of visitors to enter the crash site at a rate of $1 (equivalent to about $13.60 in 2015) for each automobile and 25¢ per pedestrian as well as 10¢ for a drink of water.

On 17 September the Milwaukee Sentinel reported that 20 Department of Justice operatives had indeed been summoned to the site and that they along with an unspecified number of federal and state prohibition agents had visited private homes to collect four truck loads of wreckage along with personal grips of several crew members and a cap believed to have belonged to Commander Lansdowne. Lansdowne's Annapolis class ring had also been thought to have been taken from his hand by looters as it was not then recovered-it was found by chance in June 1937 near the crash site # 1. No one was charged with any crime.

Inquiry
Official inquiry brought to light the fact that the fatal flight had been made under protest by Commander Lansdowne (a native of Greenville, Ohio), who had warned the Navy Department of the violent weather conditions that were common to that area of Ohio in late summer. His pleas for a cancellation of the flight only caused a temporary postponement: his superiors were keen to publicize airship technology and justify the huge cost of the airship to the taxpayers. So, as Lansdowne's widow consistently maintained at the inquiry, publicity rather than prudence won the day. This event was the trigger for Army Colonel Billy Mitchell to heavily criticize the leadership of both the Army and the Navy, leading directly to his court-martial for insubordination and the end of his military career. Heinen, according to the Daily Telegraph, placed the mechanical fault for the disaster on the removal of eight of the craft's 18 safety valves, saying that without them he would not have flown on her "for a million dollars". These valves had been removed in order to better preserve the vessel's helium, which at that time was considered a limited global resource of great rarity and strategic military importance; without these valves, the helium contained in the rising gas bags had expanded too quickly for the bags' valves' design capacity, causing the bags to tear apart the hull as they ruptured (of course, the helium which had been contained in these bags became lost into the upper atmosphere).

After the disaster, airship hulls were strengthened, control cabins were built into the keels rather than suspended from cables, and engine power was increased. More attention was also paid to weather forecasting.

</snip>


5 replies = new reply since forum marked as read
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94 Years Ago Today; Navy zeppelin USS Shenandoah destroyed in squall over Ohio (Original Post) Dennis Donovan Sep 2019 OP
The crash site of the USS Shenandoah today... Javaman Sep 2019 #1
Oh, yeah..big family folklore. luvs2sing Sep 2019 #2
The sad thing about the USN rigid dirigibles is they always killed their biggest proponents... Dennis Donovan Sep 2019 #3
Today I learned the Navy once had Zeppelins. crickets Sep 2021 #4
The home of the Shenandoah High (Zeps) doc03 Sep 2022 #5

luvs2sing

(2,220 posts)
2. Oh, yeah..big family folklore.
Tue Sep 3, 2019, 08:55 AM
Sep 2019

Several relatives on my dad’s side who lived in that area claimed to see her go down. My grandad on my mom’s side saw her fly over an hour or so before she crashed while he was working in an oil field northwest of Noble County. I heard so many stories about this as a child that I freak out whenever I see the damn Goodyear blimp.

Dennis Donovan

(18,770 posts)
3. The sad thing about the USN rigid dirigibles is they always killed their biggest proponents...
Tue Sep 3, 2019, 08:18 PM
Sep 2019

In the case of ZR-1 Shenandoah, her skipper, LCdr Zachery Landsdowne was killed when the control car broke free from the main envelope. Admiral William Moffett, another rigid airship booster, was killed when ZRS-4 USS Akron went down into the Atlantic.

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